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12-03-2014, 10:22 PM
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#15
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Senior Member
Monaco Owners Club Thor Owners Club Ford Super Duty Owner
Join Date: Dec 2006
Location: Victoria, Texas
Posts: 248
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I put some silicon sealant in the "V" notch where the wire enters the motor to seal out water. The firs motor I had only lasted until the first rain and the armature rusted and seized up.
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Larry & Doni
2015 Four Winds 31W E-450
South Texas Renegades FMCA F376075
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12-07-2014, 05:45 AM
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#16
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Senior Member
Join Date: Aug 2008
Location: Georgia
Posts: 8,638
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Quote:
Originally Posted by danes-on-tour
I got the new motor today and it looks exactly like you showed/told me.
I have tested the fit, and no modifications will be needed to get it into the roller. Maybe Carefree have listened to user comments and have shaved a bit of the offending bracket.
This is what the roller looks like and where the motor slides into.
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Did you change fabric also? I just removed end cap pulled the motor and put in new one. Then set travel length and done.
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2007 Fleetwood Revolution LE 40V
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12-07-2014, 06:02 AM
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#17
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Senior Member
Monaco Owners Club Texas Boomers Club
Join Date: Feb 2008
Location: Denmark and Spain
Posts: 2,030
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No - I didn't change the fabric. It is not warn to the extend that I need that.
I couldn't pull the motor out by jyst removing one end cap. I had to take both ends off.
First motor they send me was "dead". I am currently waiting for a replacement.
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The Great Dane
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05-25-2015, 06:11 PM
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#18
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Senior Member
Newmar Owners Club
Join Date: Apr 2010
Location: Chico, CA
Posts: 532
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Door awning gone bad
Good afternoon:
I found this thread with the same door awning problem Henrik had. Removal of the awning and replacement of the motor was easy.
I know this thread a few months old, but hope someone may have some ideas.
The problem I'm having is getting the new motor to operate. I tried to test the motor before I reattached the awning to the coach by hooking it up to the coach wires from the awning switch. I get a click when I hit the awning switch, but no motor turning. I hooked the motor directly to 12V on my car and everything worked great at both in and out motion. Checked the voltage at the connection from the coach and I get 13V. Could the voltage be too high for the Carefree motor or might I have a bad motor?
Thanks in advance for the help.
Mike
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Mike G
2019 Newmar Dutch Star 4018 - Freighliner
2022 F150 Platinum or 1973 Toyota FJ40
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05-25-2015, 10:35 PM
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#19
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Senior Member
Monaco Owners Club Texas Boomers Club
Join Date: Feb 2008
Location: Denmark and Spain
Posts: 2,030
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Mike - the first motor that I got didn't work at all. I also ended up testing it using my car battery, and it wouldn't move. I did the same to the replacement, and it worked fine when connected to the car battery.
I would be surprised if 13V is too much because your house batteries would have supplied that all the time when fully charged. The only thing that I can think of is that the 13V does not reach the motor when you operate the in/out switch in the motorhome. Mind you - I am far from being an expert on this subject.
I hope that you get it sorted out
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The Great Dane
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05-25-2015, 11:54 PM
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#20
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Senior Member
Monaco Owners Club
Join Date: Jun 2009
Location: Milwaukie, Oregon
Posts: 276
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More then likely the voltage is dropping below 12 volts when the switch is applied. You will need to connect a volt meter to the wires with the motor hooked up. A bad switch, loose connection, even a bad fuse that looks good. Good luck
Rich
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Rich & Joan + Zach Parti Miniature Schnauzer
2006 Beaver Monterey
2004 Monaco Cayman
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05-26-2015, 06:57 AM
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#21
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Senior Member
Newmar Owners Club
Join Date: Apr 2010
Location: Chico, CA
Posts: 532
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Thanks for the input guys.
Rich. I checked the voltage where I am splicing in the motor. 13V forward and reverse when the switch is applied. I'll check it with the motor spliced in. Didn't think of that.
Henrik. I'm hoping the motor is not bad, but I may need to remove it again and bench test it.
Thanks again for the replies.
Cheers,
Mike
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Mike G
2019 Newmar Dutch Star 4018 - Freighliner
2022 F150 Platinum or 1973 Toyota FJ40
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05-28-2015, 11:28 AM
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#22
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Senior Member
Newmar Owners Club
Join Date: Apr 2010
Location: Chico, CA
Posts: 532
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Talked to Carefree. They thought the limit adjustments may be off, but not the case. I do have an extra motor that was originally sent without the "forks" that engage with the awning roller tube. I did a bench test and confirmed that motor is good. I'll take the awning apart and replace the motor as soon as I can. That should solve the problem.
Thanks again for the tips guys.
Cheers,
Mike
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Mike G
2019 Newmar Dutch Star 4018 - Freighliner
2022 F150 Platinum or 1973 Toyota FJ40
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05-30-2015, 08:04 AM
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#23
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Senior Member
Monaco Owners Club Holiday Rambler Owners Club
Join Date: Jul 2006
Location: Cornville, AZ
Posts: 1,105
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Mike A number of years ago we had a problem with the door awning. The motor had failed and we had it replace at a RV shop under warranty. When they got it all done the new motor would not work. They removed the awning and bench tested it and it worked fine. Turned out there was an extra tab on the motor that was touching ground on the RV when the awning was installed, so it would not work. They clipped off the tab and everything worked fine. Just another thing to look at.
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Dave & Jeri
06 Holiday Rambler Endeavor
TOAD 15 Lincoln MKX
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05-31-2015, 02:16 PM
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#24
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Senior Member
Join Date: Jun 2011
Location: FL
Posts: 11,452
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Quote:
Originally Posted by R&J
More then likely the voltage is dropping below 12 volts when the switch is applied. You will need to connect a volt meter to the wires with the motor hooked up. A bad switch, loose connection, even a bad fuse that looks good. Good luck
Rich
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Dead on. High voltage is NOT the problem. I suspect when you reconnected that the connection was defective. Since it ran when connected to the battery directly you must have a low voltage problem.
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Certified Senior Electronic Technician, Telecommunications Engineer, Telecommunications repair Service Center Owner, Original owner HR 2008
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06-01-2015, 07:22 AM
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#25
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Senior Member
Newmar Owners Club
Join Date: Apr 2010
Location: Chico, CA
Posts: 532
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Problem solved.
Like Henrik, bad motor. I used the first motor they sent, moved the parts missing from the second motor and installed the first motor. Now it works fine.
Thanks all for the input.
Have a great week.
Mike
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Mike G
2019 Newmar Dutch Star 4018 - Freighliner
2022 F150 Platinum or 1973 Toyota FJ40
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