Well after all I've done with this issue turns out there were several issues biggest being my fuel filter housing. Had a Winn electronic filter system that was undersized for the flow the engine required. Changed it out to a large spin on type and coach has more Power than it ever has!!
Went 350 miles this weekend to hershey pulling my stacker through the mountains set cruise at 75 never got above 200F. Finally solved my problem. Good news about it is every possible filter and service has been done trying to pin point it.
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